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Many chargers have their operating switches mounted directly on the unit’s printed circuit board (PCB). These switches are operated by panel mounted buttons. Over time, the switches can become clogged with dust and dirt, which may cause them to work poorly and unreliably. Eventually the charger can become quite difficult and unpleasant to use, requiring a high pressure on the buttons for any kind of response.
This short article describes how I restored my Lipo capable Mercury EX charger back to full health simply by cleaning its PCB mounted switches. It turned out to be a very quick maintenance job which yielded a great result. The same technique may be also be applied to other chargers such as the Super Nova, FMA Super Nova and many others.
This work requires the charger to be opened up. Clearly this will invalidate the manufacturer’s guarantee, so it’s probably only of interest for old equipment. My charger was well out of guarantee and wasn't working properly so I nothing to lose.
Equipment
Very little equipment was needed for this project. I used the following:
Suitable screwdrivers.
A spray can of switch cleaning fluid (such as Servisol) with a suitable
applicator tube. This is available from electrical supply shops for £3
or so.
Eye protection
NB Make sure that you use switch cleaning compound and nothing else – sprays such as WD40 oil are totally unsuitable.
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Safety precautions
I always feel it’s important for health not to breathe in any vapours,
overspray or splashes from synthetic compounds such as paints, glues or
the switch cleaning fluid I used for this job. I have an efficient extractor
fan plus an extract hood at my workshop, but I could also have chosen
to work outside if these had not been available. When spraying the cleaning
fluid I also wore eye protection in case of unexpected splashes.
The procedure
I’d not dismantled my charger before so I was not sure where to
start. I decided to begin by detaching the charger’s end panels.
However, this didn’t provide enough access to the PCB, so I removed
the front panel as well. In my case the four screws at the panel corners
had to be removed to accomplish this. I placed all the screws in a suitable
receptacle so they didn’t get lost.
Removing the front panel. |
Upon lifting the front panel, I found that it would not come away very far, which made access to the PCB still difficult. This was because the fan, which was attached to the underside of the front panel, was still connected to the PCB by a short length of cable. I disconnected this, which allowed me to fully remove the front panel.
The front panel also housed the three black plastic buttons which operated the switches directly below them. I now had the required easy access to the PCB.
Inside, I found that the electrical switches which operated the charger were, as expected actually attached to the printed circuit board (PCB). They were operated by the three black plastic buttons located on the front panel.
Inside the charger. The front
panel to which the fan is attached has been completely removed.
The end panels have been left loose for now. The PCB is low down
in the case. |
To clean the switches it was necessary to direct some switch cleaning compound (definitely not WD40!) into to the switch’s interior. I first tried to do this by spraying in the general direction of the switch, but I wasn’t confident that any of the fluid had actually reached the switch’s interior.
By using an applicator tube I was able to apply the cleaning fluid under pressure directly into the switch. Only in this way was I confident that some of the cleaning fluid had got right inside the switch and, I hoped, dislodged any dirt that had accumulated there. I made several short squirts and to assist the fluid in reaching the switch contacts, I felt it helped to wobble the switch while spraying.
Switch cleaning compound is
sprayed at the PCB mounted switches. These are the small black square
shaped items. This picture shows my first attempt, without an applicator
tube. This didn't work well. |
After applying the fluid, the charger was left outside for several hours to dry out. The fluid evaporates quickly so this time period could probably have been reduced to just a few minutes or so, but I wasn’t in any rush. In the meantime I took the opportunity to clean up the charger's yellow front panel. I then re-connected the fan to the PCB, and replaced the front panel, making sure that the plastic buttons mated correctly with the PCB mounted switches.
The end result
Upon testing it, I was delighted to find that the charger worked beautifully
again, requiring only a very light press of the buttons for a positive
response. Excluding drying time, the total time taken for this job was
only a few minutes. The job was so quick and easy that I wondered why
I hadn’t done it much sooner! And of course in these recessionary
times, repairing equipment instead of replacing it is a particularly attractive
idea.
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